Hello Friends,
Thank you so much for your support and responses. Adding some more photos.
Before cleaning
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Flywheel rust
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After some sanding with very fine emery paper the rust was removed. There is discoloration but the rust stopped leaving any mark on the emery paper and surface is now smooth and free of uneven rust formation.
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Cleaning and putting the transport back together.
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The tension arm felt was replaced with a small piece of felt cut out of a polishing wheel I had. This was the closest material I could find to the original. It works perfectly. Note that the felt has to be cut in such a way that it should only touch the bottom part of the supply reel hub.
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Restoring the rollers took a lot of time. I washed them first in water. Then too, the brown color and the glaze remained. So the rolled was assembled back on to its arm. Then I got super fine abrasive sheet (2000 grit) from polishing shop. Kept this sheet flat on the table and rolled the pinch roller over the paper while pressing the roller down. If you attempt this make sure that the roller rotates freely even when it is pressed. The movement should be gentle straight lines back and forth. As the roller is rolling over the paper, it doesn't remove much of rubber. But this is the only way because, if the paper rubs against stationary roller, it will go out of shape. Rolling will remove the surface non-uniformity and dirt beautifully. So after a lot of rolling I got it very clean. All the lines and cracks disappeared and the surface became soft as new. You have to do it slowly and patiently. This is what I have got.
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The next step is to adjust the guide heights. For doing this in the proper way, an M-300 gauge or an exact replica WHS-300 (what I have is required).
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The purpose of this alignment is to have the guides and the rollers in the exact position where the tape would be when they travel across the head. Improper alignment will cause miss tracking and in worse cases, the tape edges will be chewed.
Once this is done, it is time to mount the head block in place and adjust PB and Rec head tilt. The tilt is to make sure that the head surface is exactly parallel to the tape surface when it comes in contact with the tape. This is required for even pressure of the tape on the head in both L and R channels.
Miss alignment of tilt can cause unequal freq response between L and R, Tape skewing and non uniform head wear in the long run. The tilt is also called as Zenith.
The top screw in the head block adjusts tilt. The bottom one is used for track height. The height is only approximate setting for now because it require the height alignment tape and we need to monitor the audio while doing it.
Once the tilt is adjusted, the center pulley has to be inserted so that while aligning the height later, the tilt setting won't go wrong.
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The next thing to do is the head stroke setting. This determine how much the head penetrate into the cassette during play and record. This is a standard form DIN and Philips. The gauge is precision machined to these standards.
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It is almost time to put the work so far to test. So only the power section of the transport is connected. The leaf switch which was on the door holder assy has to be closed by putting a light rubber band around it. Also the ground connection has to be given to the cam drive motor with a wire(I made one with clips on both sides). This connection is required now because the transport is kept outside.
The first thing is to ensure that the tape path is correct and the restored rollers are behaving properly. I have a DIY cut open tape, which is a wild imitation of the Nak mirror tape. That one is loaded and I set it to play. :yahoo::yahoo::yahoo:
The tape runs rock steady.
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Now I can confidently use my alignment tapes for the remaining work.
But before that I need to do some work I had kept pending. First to fix the broken post in the right bottom. A 15mm M3 machine screw, a 10mm brass spacer and a washer is used for this job.
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The next is to fix the soft eject. The feel of the eject was unlike my other naks. On inspection I found that rubber piston inside the vacuum pipe was torn. Someone who serviced this before was brut enough to pull it out without pressing the eject lever. This is the only way it can get torn. Because it is full of grease, no glue will stick on it. I need to wash it thoroughly first.
I am out of energy today. So I will continue this tomorrow.....
Thanks for reading...